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rusteee

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Posts posted by rusteee


  1. Hey Adrian, I did have the cooler and lines done when I had the box and converter rebuilt as that was causing the problem all along and AAutomotive decided to rebuild instead of diagnosing the fault properly, not sure if it would fail in that short amount of time? Mind you didnt think the box would fail in such a short amount of time either. It was completely blocked when we pulled it out so replaced the whole thing, the lines and the radiator.

     

    This beast is going to be like new by the time you are finished with it! Good work


  2. 29 minutes ago, Eagle said:

    Damn, hopefully its electrical rather than the internals. Has the transmission even been worked on?

    I hope its no major Adrian. Thats the third gearbox in that beast and millionth torque converter which both had been fully rebuilt so be suprising if it was internal. Keen to see what the issue is, hopfully just some bad connection somewhere in the line


  3. Car is looking mint! Always loved that colour. Get a few K's in during the holidays? Be a bit odd if it is the centre drag link is knackered, I used genuine Lemforder drag link, tie rods and pitman arm when all the other suspension parts were done. Drag link alone cost me around $800. Be keen to see what it looks like when it comes off.


  4. Nope. still have the mismatched lights haha. have some updates though! check the progress on my projects thread russell!

    I'll have a look through those ones Martin gave me, and see if can make up a complete 1. I had a quick geez through your thread the other day, that car is awsome man!! I'll go have another look now

    • Like 1

  5. Unsure, but whatever it was was drawing between 900mA and 1.3A lol. He got the same figures as me after pulling out all the fuses for the phone, lights etc etc once the car had gone into sleep mode. I'll check tommmorow when I pick it up, but must be some modules or something that it kept on? He did mention something about centre console lights, I wasn't even aware there was any.


  6. Well turns out the GME is indeed faulty. Which is a bastard as thats the last solution I had come up with. I assumed they were going to plug in the tester and see if it was sending everything to sleep as I had discussed with them over the phone, but no. So 4 hours at $100 an hour of doing everything I had already done, they had confirmed it. Replacment ordered and on the way. I suppose the small bonus is he said I was bang on with my diagnosis hahaha sheeeeit. All ready for the new owner whom ever it may be lol

    • Like 1

  7. Cheers for that, but after hours of tearing my hair out, I gave up and have taken it in to the auto sparky today for them to sort out. After pulling every fuse in the glovebox, boot, aux fan and heater fan fuses, disconnected alternator and various other bits and pieces it was still drawing between 900mA and 1.3A all day yesterday. Will update when they find what the problem is.


  8. Hi guys

    Thought I'd put it in a new one, save sifting through the other thread. I thought I had it sussed but appears not. In a nut shell, have been having issues with with the E39 540i, battery draining over 3-4 days of sitting. In a nut shell, have replaced battery, alternator is charging 100%, FSU is disconnected, all radio fuses and display, phone, stacker etc all disconnected, heater panel physically disconnected, after market amp, auxillary fan, alternator, interior lighting, seats, mirrors, window switches all currently are disconnected or have the fuses pulled. I have been through and pulled every single fuse 1 by one which made no difference. The car goes to sleep (the little park light goes out), but there is something that is drawing just over 900mA and I cant for the life of me figure out what it is. Does anyone have any other ideas?

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