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BreakMyWindow

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Posts posted by BreakMyWindow


  1. 15 hours ago, The H. Behemoth said:

    Dear friends, Its amusing and interesting, So much hate and so much misinformation, tall tales and even lies. Monty Python would be proud and one can certainly reach the yellow press with such. In the end I can only wish some of you the very best. :)

    I must respond and say, last I checked this 'moron' was on the German newspapers and was meeting the mayor of the city for his contributions: https://wilih.de/neu-stuttgarter-spendet-10-000-einwegmasken  - These days hes hanging out with some higher ups at some very big companies in the automotive sector and I heard his company has gone international worth a few million and 6 branches around the world.  Last I checked his company was one of the 7 in the world doing what they did. Things crazy morons do.

    He even gave away a car above to a Charlie from Christchurch whose a member of this forum and he can confirm the false story above, he had run the car low on oil (after a 1200KM Drive back to South Island) and he confirmed it, and he still had a year time to pay. Dont know many people doing that.  

    I must forward this topic to the former director of the MB Kompressor department, so that moron who lives 2 houses away from him, can sit down over a nice evening and have a laugh and remind themselves that the Eaton was only the second option as the original choice was the German designed and lisenced by Ogura SC14 (Wankel AG - https://www.wankel-ag.de/seite1_e.html) and was not an option due to low manufacturing capacity (Toyota buying them all up)

     

    Back on topic,

    We all should respect the beliefs others have, but science is science and has no place but facts. Below are the lowest numbers seen this year. Before and After.

    Much love and warm regards.

    20200923_015418.jpg

    20200923_015459.jpg

    2387722255_d58abca988_b.0.0.jpg

    • Thanks 1
    • Haha 5

  2. Don’t think the van was parked where it goes from 3 to 2 lanes. Looks like it was parked on the 2 lane down hill section shoulder which is the best, but obviously not in this case, place to catch speeders on sh18. Maybe was parked initially under the bridge, or possibly before as the van took a big hit. 891234A5-42C5-49A3-9428-9B2C21819BF1.jpeg


  3. Bit more fiddling with vanos stuff. Adjusted the cam timing so that the alignment marks are perfect. The efforts paid off as the vanos tests now consistently pass. Below are pics of how making the slightest adjustments affect the test results. 
     

    Also fitted a new radiator and renewed all the front coolant hoses.

    42C23C3C-A8EC-4A4D-8DD5-A9C740E55C50.jpegB72705D0-F338-461E-81A7-63438617581D.jpeg718D53FE-A677-4F73-9F57-C3CEFF652164.jpegF2C6F278-B540-401B-8B59-9A5C11E0026A.jpeg


     

    • Like 5

  4. Slow progress getting it back on road. All parts arrived to be able to fully re-assemble, but noticed that there was evidence of leaking from one of the plenum oil return hoses. Being that all 3 were original 1999 date coded parts along with the radiator, hoses and fan clutch I decided to renew all of these given their age and reluctance to have to re-visit working on this engine any time soon. So another week or 2 and those parts should arrive. In the mean time i’ve fitted all new idler pulleys, new gen bmw alternator, replaced the ac pulley clutch bearing and re-installed the bank 1 upper chain cover.

    644D5B97-A53F-4A59-B27C-7F346E030AAC.jpeg

    4B309325-B4C8-43E1-B9B3-D672B054B4FA.jpeg

    • Like 4

  5. Time for some maintenance in the engine bay. Leaking valve cover gaskets and a good attempt to sort an intermittent engine rattle that comes and goes and has been there since owning the car.

    Thought the timing might be slightly off but it was perfect, but did notice the main chain sprocket on the b1 intake came was off by 1 tooth compared to b2. Vanos should compensate for this easily, but it just meant that the intake cam couldn’t reach its full range of travel on advancement. Certainly didn’t feel down on power but good to correct this while it’s apart. Suspect po’s engine builder got this wrong and i did not notice way back when I refurbished the vanos units. 

    The secondary air pump line bracket on b1 was loose due to the threads in the upper chain cover being stripped out. I think that may have caused the rattling but will have to see when it’s back on the road.

    4 new cps’s to go in and a set of fresh plugs and filters. I forgot how much of a c u n t changing cps’s out on the s62.

    Ordered a new alternator too as the lights were flickering at idle and bearings starting to get grumbly. New belts and idler pulleys to boot also. 
     

    Good to see after nearly 6 years of ownership it’s still very clean inside and the chain guides are mint.

     

    EFF8AD57-252C-45EA-A2ED-F7FED8F95E82.jpegEF02817E-CCE3-492C-9EC9-24090B23AACA.jpeg8F6A128F-912C-4DCD-883B-CC035F02321C.jpeg30CC6311-3F1A-4E68-B3DA-75E6F8822053.jpeg91493A8C-AD47-4BB8-A554-F6E2472EC6AD.jpeg

    • Like 8
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